Notes |
This was supposed to be a dual-zone installation, annular POF-24 (260-340), open-hole POF-25 (540-600). Apparently there were some major problems during construction of the well. According to internal documentation POF-24 had been clogged since the time of installation 2/20/2008. POF-25 also acted clogged (strange hydrograph), so both wells were de-activated. In 2012, POF-25 was logged. It was found that the casing was obstructed/severely bent @446, and could not be logged past that point. Any data collected was not usable. |